Tomorrow’s workday will be at Muckleford, meeting at Maldon 7.45am then by Walmer Rd Crossing from 8.15am.
Maldon Yard

Today the Down end 3 Road turnout at Maldon received some attention.

We had one timber to replace from some months back when we put the air and water lines in, however while there, we decided to do a proper job and replace a few more. 6 were replaced in total, a combination of new and 2nd hand.

We also replaced a broken rail, unfortunately in these old turnouts, the rails are so worn that breaks occur very easily, thankfully we have none like this in the mainline any longer, there just relegated to the depths of Maldon Yard.


We also managed to fit in some drainage works, which will hopefully stop the water pooling in the area like it has been.
The exact details of Thursday’s workday are yet to be determined, however it’ll likely be a day down at Muckleford preparing for the Wamer Road Crossing Rebuild.
Tuesday Workday
Tomorrow’s crew will be knocking over a few more odd jobs, we’ve got a few jobs to complete around Maldon first up, so we’ll be meeting there from 8am.
Ticking things off the list

The majority of the list of to dos following yesterday’s track walk are now complete. The first being the abutment at Muckleford Creek, where 2 buckets of rock were applied and compacted in, while another couple of buckets of dirt were used to shore up the sheeting to ensure it doesn’t settle too much further.

While down by the creek, we removed and filled a bit of rock and scour to ensure an unweary vehicle driver coming to grief while crossing the stream.

The big old bridge pile hole took about 1/2 a bucket of gravel to fill, with lots of ramming from the digger to fill any big voids, it seems to have solidify nicely.


4 sleepers were replaced between Pipeline Crossing and Bendigo Rd, with that removing the gauge faults.
We’ve only got two major faults remaining, both of which are easy fixes and we’ll get onto them next week, one at Muckleford and one in Castlemaine Yard. Almost all the minor faults were also corrected today (mainly bolt tightening), leaving a nicely short list to urgent things to do.

We even found time to get a heap of tamping done too, until the tamper went out in protest! Easy fix, but certainly a Monday job.
Check back Monday for details of Tuesday.
